Wednesday, October 28, 2009
H-31
Today, I solved one problem, but encountered another. I fixed my issues with the light sensor by testing the light level sensed with and without a ball, and that part of my robot is working now. This allowed me to make my first full test, and as I was doing it, I discovered that my ejection method doesn't work as I expected it to. This should be fairly easy to fix, and I think I will be able to finish tomorrow.
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