Sunday, October 18, 2009

H-24

The king climber project didn't go very well for me. When I ran my robot on flat ground it worked and moved. But then when I placed it on the steps it made it up the first one or none at all and then just stopped. The first trial didn't work because of the light sensor reflecting underneath the lego and hitting black (making it stop. so i guess at least it did that...) and I think kourtney had this same problem for one of her trial runs too. And the other problem that I had was that I would get it up one step and then there would be this annoying clicking of the gears and one of them was moving faster then the other. This is my fault, as I should have checked for that mechanical problem beforehand.

No comments:

Post a Comment